Analiza przyczyn pęknięć w złączu rura płuczkowa-zwornik w wiertnictwie
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Abstract
W pracy omówiono przyczyny występowania pęknięć złączy rura-zwornik podczas eksploatacji rur płuczkowych. Na podstawie badań stwierdzono niewłaściwy sposób wykonania złącza elektrody zostały źle dobra- ne i sprzyjały powstawaniu pęknięć. Ujawniono również wykorzystanie do produkcji rur płuczkowych niewłaściwego gatunku stali. Dla porównania przedstawiono zmiany właściwości i mikrostruktury złącza rura-zwornik wykonanego metodą zgrzewania tarciowego.
Analysis of the causes of cracks in the drill pipe-nipple joint region
Abstract
The paper presents analysis of the causes of cracks in the pipe-nipple joint region of the drill pipes occurred during service. The results of performed examinations showed the wrong way of making the pipe-nipple joint by welding instead of friction welding. In addition, electrodes used for welding were incorrect and favored crack nucleation and propagation in the heat affected zone of nipple joint. Also discloses the use of the drill pipe of the wrong steel grade. The changes in hardness and microstructure of the pipe-nipple joint properly made by friction welding were shown for comparison.
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